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  1. #106
    Join Date
    Nov 2008
    Location
    Perth WA
    Age
    71
    Posts
    5,650

    Default The Arm that raises and lowers the Table

    The upper end of the arm is held in place in the Z slide casting with a 3/8" diameter steel pin. I initially thought that the pin had been driven in place during assembly at the factory and that its removal was going to be tricky. Wasn't so. Woodfast knurled the pin to ensure a tight fit but use or maybe abuse caused the pin to bell mouth the hole in the cast iron arm thereby loosening it.

    IMG_20211030_092942158.jpg IMG_20211029_134151029.jpg IMG_20211030_095152881.jpg IMG_20211030_095504896.jpg

    I bored the hole out to 10.1mm to remove effects of the bell mouthing and then made a stepped pin from 4140. To facilitate secure fixing and future removal of the pin I tapped the casting to accommodate a 3/16"BSW socket grub screw and milled a flat on the pin to ensure easy removal. A few fiddly setups... The stubby stepped pin enabled the use of the microscope to centre the existing hole. The boring head uses 10mm shanked tools. The boring bar is 4mm in diameter and held in a 10mm shanked ER11 chuck.

    IMG_20211112_151914680.jpg IMG_20211112_152008679.jpg IMG_20211112_152633426.jpg IMG_20211112_154554033.jpg IMG_20211112_155131071.jpg

    Fiddlier for drilling and tapping.

    IMG_20211113_101239038.jpg IMG_20211113_113630621.jpg IMG_20211113_115502674.jpg

    I removed the rust from the castings with 'Rust-Off' then coated them with Rustoleum satin clear.

    IMG_20211113_141532599.jpg IMG_20211113_141457512.jpg IMG_20211113_141653650.jpg

    BT

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  3. #107
    Join Date
    Nov 2008
    Location
    Perth WA
    Age
    71
    Posts
    5,650

    Default The Sheetmetal Base

    The base was riddled with holes as a result the attachment of switch gear and conduit. Twenty one 1/8" self tapper holes and four 1/4" bolt holes. I asked for suggestions as to how to neatly fill the holes over in the Metalworking forum and most suggested MIG welding the holes closed. Not owning a MIG welder, I thought a reasonable result might be achieved using Devcon Steel Epoxy or JB Weld's equivalent. I ended up using JB Weld.

    The underside of the base was also heavily rusted so I used my 'Air-Boy' sandblaster to clean up the base and all the fixing holes. The photo below is of the Universal in the back of Bob's van when we collected it from the shipping container.

    IMG_20200717_151619596.jpg IMG_20211126_144044227.jpg IMG_20211126_091427901.jpg

    After blasting the underside I painted the steel with Balchan Zinc Rich Cold Galvanising paint in a rattle can.

    The screw holes all had a thread cut by the screw so I thought the thread and the sandblasting would provide a key for the epoxy. I backed the holes with four layers of masking tape and overfilled the holes. Once cured. they were sanded flush and swiped over with body filler, sanded again and overcoated with Balchan Etch Primer, also rattle canned.

    IMG_20211105_160449197.jpg IMG_20211105_154355489.jpg IMG_20211125_161542584.jpg IMG_20211126_091601606.jpg IMG_20211127_111527211.jpg

    I was going the fill the 1/4" holes with an epoxied in place, stepped steel plug but instead I ran a tap through the holes and filled them as per the others.

    IMG_20211126_155718632.jpg IMG_20211126_155757808.jpg IMG_20211126_160358186.jpg

    I'm happy so far with the results but there is a lot more work to do before I haul out the spray gun.

    IMG_20211127_095902714.jpg IMG_20211127_095544413.jpg IMG_20211127_102508072.jpg

    BT

  4. #108
    Join Date
    Feb 2006
    Location
    Perth
    Posts
    27,790

    Default

    Looks good, but hot day to be doing this in the shed - looks like you might have even been outside?

  5. #109
    Join Date
    Nov 2008
    Location
    Perth WA
    Age
    71
    Posts
    5,650

    Default

    Quote Originally Posted by BobL View Post
    Looks good, but hot day to be doing this in teh shed - looks like you might have even been outside?
    Outside the shed with the sun beaming off the Zincalume!!! The epoxy and the filler sure cured quickly !

  6. #110
    Join Date
    Oct 2018
    Location
    Dandenong Ranges
    Posts
    1,892

    Default

    Hi AB. Where did you purchase you sand blaster? That looks pretty handy.

  7. #111
    Join Date
    Nov 2008
    Location
    Perth WA
    Age
    71
    Posts
    5,650

    Default

    Quote Originally Posted by Mountain Ash View Post
    Hi AB. Where did you purchase you sand blaster? That looks pretty handy.
    Hello MA,

    I purchased it at least 15 years ago from Toolmart in Victoria Park for $59.95. They are still available and haven't gone up that much since then - AIR BOY Sandblasting Gun | Total Tools

    Handy for small stuff. Removing the rust from the underside of the Universal's base was a time consuming task. Three hours worth!

    Bob.

  8. #112
    Join Date
    Oct 2018
    Location
    Dandenong Ranges
    Posts
    1,892

    Default

    Thanks Bob. I guess the sand has to be pretty dry too.

  9. #113
    Join Date
    Nov 2008
    Location
    Perth WA
    Age
    71
    Posts
    5,650

    Default

    Quote Originally Posted by Mountain Ash View Post
    Thanks Bob. I guess the sand has to be pretty dry too.
    I used garnet I purchased from Fiora Machinery at the time of the Air-Boy purchase so I reckon it would have been dry enough !

  10. #114
    Join Date
    Nov 2008
    Location
    Perth WA
    Age
    71
    Posts
    5,650

    Default The Painted Base.

    After priming the bare metal with etch primer and the painted surfaces with grey primer along with some primer filler, I painted the base using spraying enamel colour matched by and purchased from Global Autocoat located over here in Bentley.

    Initially I used gloss enamel but the combination of a hot day, nearly 34C, and the paint's swift drying lead to problems with overspray and orange peeling, so I repainted the base on a cooler day using a mixture of three parts gloss to one of matt and the addition of mineral turps to the enamel thinners to retard the drying. Worked OK.

    IMG_20211206_054617922.jpg IMG_20211206_055104010.jpg IMG_20211206_155300488.jpg

    Primed and gloss painted.

    IMG_20211216_072111554.jpg IMG_20211216_072405813.jpg IMG_20211216_072317955.jpg

    And with the gloss knocked off.

    BT

  11. #115
    Join Date
    Feb 2016
    Location
    Canberra
    Posts
    5,124

    Default

    A little MIG welder is an excellent tool to have.

    Perfect for these jobs.

  12. #116
    Join Date
    Nov 2008
    Location
    Perth WA
    Age
    71
    Posts
    5,650

    Default Only Cosmetic.

    No machines involved, just took a while.

    The large 'Woodfast' badge fixed to the motor access panel was in a sorry state so I thought I would have a go at improving it. If the badge was flat it could probably have been airbrushed and sanded back but its slight doming prevented that. My daughter suggested masking the raised letters using a paint on mask and I asked the fellow at MAS Hobbies, where I purchased the paint, if masking was an option. He asked if I had a steady hand instead!!!

    The Revell No.31 'Fiery Red' gloss paint I used is close to a perfect match to RAL 3000 'Flame Red', the colour in the RAL fandeck closest to that used by Woodfast on the smaller, better condition badges.

    I thinned the enamel about 6:1 with enamel thinners and used a tiny brush to cut in. Thinned because I didn't want a thick build up of paint around the letters. The paint in some cases ran along the little recessed gully formed at the edges of the letters.

    I used a wider sable brush to apply unthinned paint to the open expanses. I found it impossible to avoid brush marks so I opted for a stippled finish, dabbing the paint on. The black ring has some deep scratches which I left as is, some things can't be turned into silk purses.

    IMG_20211105_160508157.jpg IMG_20211219_154652260.jpg IMG_20211219_154848513.jpg IMG_20211221_084847621.jpg IMG_20211221_084918580.jpg IMG_20211221_085245385.jpg

    IMG_20211221_110542567.jpg IMG_20211221_114705122 (1).jpg IMG_20211221_114956711.jpg

    IMG_20211228_084835294.jpg

    BT

  13. #117
    Join Date
    Feb 2016
    Location
    Canberra
    Posts
    5,124

    Default

    I might have been inclined to simply spray clear enamel over that badge and left it manky and wabi-sabi..... everything else perfect other than the badge

    Magnificent!

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